ChaneRZ
1000 Posts Club!
Exxon is pretty good. Use up your current tank all the way to near empty and then refuel.
Definitely disconnect the battery for about 10 minutes with the doors locked and the key outside of range. I am not saying that will fix your problems. However, it can't hurt.Thanks everyone for all the help! I thought I was picking good fuel. We really have two main fuel suppliers in town, Holiday and Casey's. I try to only go to Holiday stations that have a dedicated pump for 91 that also doesnt have any ethanol. A lot of our stations have 91 with up to 10% ethanol. I will try to fill at a different Holiday for the next tank. I am at over a half tank left right now.
I installed my BMS intakes yesterday and did a few more data logs. It is still pulling timing, but this time it doesnt seem to be getting quite as high consistently. So the only change is just adding intakes. I might try disconnecting the battery today. I will post on our local car group page on FB to see if there is anywhere that has generally better quality fuel. I have never trusted Costco, but they do have 92 in town here.
Is timing the main thing we want to look at in these logs?
I do have E85 at a few different places around town. I had not really thought much of doing a blend because I wasnt sure I wanted to mess with the mixtures.Definitely disconnect the battery for about 10 minutes with the doors locked and the key outside of range. I am not saying that will fix your problems. However, it can't hurt.
The timing is so bad with what you have right now that you really need to clear as much gas as possible out of that tank, refill it with good gas, reset the ECU and then hope that you don't have any other issues.
I had serious timing pulls like you have and still set my fastest times. However, I put some E85 in the tank with 93 Octane and reset the ECU. My timings instantly went to zero corrections and have been close to that the entire time now. Do they have E85 in your area?
Personally, I don't think it really ever hurts to reset the ECU. It may not help but I don't see how it can hurt.I do have E85 at a few different places around town. I had not really thought much of doing a blend because I wasnt sure I wanted to mess with the mixtures.
Would you recommend disconnecting the battery with this tank of gas? or wait it out and disconnect when I refill?
Not so sure about the ECU reset as it's reason for the timing fluctuations is that the octane level is so crappy that it is trying to compensate as best as it can to prevent knock (ENGINE KILLER). Think about it....resetting the ECU is not going to somehow modify the programming so once the engine runs for a bit and you don't have better gas, guess what??? The ECU is going to refer to the same table values for that octane and jerk timing all over again.......remember, the ECU is getting it's info from the exhaust via O2 sensors. Disconnecting battery is not going to re-train the O2 sensors......Personally, I don't think it really ever hurts to reset the ECU. It may not help but I don't see how it can hurt.
I appreciate your perspective monusa. I have not reset the ECU, and I agree with your thoughts on the learning aspect. It is hard because the car does feel stronger now with map 1, so it feels like it is working.Not so sure about the ECU reset as it's reason for the timing fluctuations is that the octane level is so crappy that it is trying to compensate as best as it can to prevent knock (ENGINE KILLER). Think about it....resetting the ECU is not going to somehow modify the programming so once the engine runs for a bit and you don't have better gas, guess what??? The ECU is going to refer to the same table values for that octane and jerk timing all over again.......remember, the ECU is getting it's info from the exhaust via O2 sensors. Disconnecting battery is not going to re-train the O2 sensors......
If it were my vehicle, knowing what I know now, I would put the jb4 to map 0 until I had a chance to run out the crap gas and get a fresh tank of better quality. run that through and on the next tank of GOOD gas, switch jb4 to map1, take a log or two and critique results before going any further.
I have had an engine replaced and although it was covered under warranty, not a fun situation.
Just my thoughts......
Bad gas may cause rough idle/sputtering when stock. The JB4 is an awesome device and when all aspects are in sync (plugs, gas/octane level, any other mods) it makes for a pretty fun driving experience on the Stinger.I appreciate your perspective monusa. I have not reset the ECU, and I agree with your thoughts on the learning aspect. It is hard because the car does feel stronger now with map 1, so it feels like it is working.
We aren’t saying anything different. I said run the tank out while not pushing the car at all. Then, once you have eliminated all other variables reset the ECU. That is inline with everything you stated.Not so sure about the ECU reset as it's reason for the timing fluctuations is that the octane level is so crappy that it is trying to compensate as best as it can to prevent knock (ENGINE KILLER). Think about it....resetting the ECU is not going to somehow modify the programming so once the engine runs for a bit and you don't have better gas, guess what??? The ECU is going to refer to the same table values for that octane and jerk timing all over again.......remember, the ECU is getting it's info from the exhaust via O2 sensors. Disconnecting battery is not going to re-train the O2 sensors......
If it were my vehicle, knowing what I know now, I would put the jb4 to map 0 until I had a chance to run out the crap gas and get a fresh tank of better quality. run that through and on the next tank of GOOD gas, switch jb4 to map1, take a log or two and critique results before going any further.
I have had an engine replaced and although it was covered under warranty, not a fun situation.
Just my thoughts......
Thanks for the info ChaneRZ. I read about intakes getting wet on other threads (not related to any codes) so that was my first instinct was to check them since I was driving in rain for 90 miles. The passenger intake was dry, the driver one had a couple droplets on the rubber, but the filter seemed dry. This fault looks like it is related to MAF/throttle, but we dont have MAF so I am not sure how it relates to our setup. I wonder if it was possibly traction related because I was accelerating on a turn when the car died after I let off. Then the fault came on and went into limp mode.![]()
P061B Internal Control Module Torque Calculation Performance
How to easily diagnose, repair, and info on causes of a P061B trouble code that indicates a detected internal performance error with the torque performance calculation.www.obd-codes.com
That is kind of what I was thinking as well, but everything looks good on the intake ducting. Everything is connected and tight. The filters werent wet to the touch.Check Air filters again and make sure they are NOT allowing air to get past or other contaminants to get past (dust, moisture, etc.).
This could be giving TMAP sensor incorrect readings and the shutdown/limp mode could be a result of the sensor shutting down throttle.....
Filter may in fact, be dry but what no one wants is moisture getting past the filter seal. If you take out the filter, is there excessive moisture in the housing or dust?The passenger intake was dry, the driver one had a couple droplets on the rubber, but the filter seemed dry. This fault looks like it is related to MAF/throttle, but we dont have MAF so I am not sure how it relates to our setup
I just took off both filters to check. They are bone dry and show no signs of any moisture in the intake tubing. It has been ~8 hours since I got home and put the car in the garage. I can see dried moisture on the outside of the tubing on the front of the tube, so water did get into the bay through the grill. But the moisture evidence stops at the filter seal. There is no indication that any moisture got past the seal in any way.Clamps, connectors secure? I know the code is pointing to drive-ability issues but going into limp mode is basically the engine/ecu saying they don't agree with what is going on from the time air comes in to the time it goes out the exhaust.
Educated guess is that the something "wrong" is happening just before combustion....
Filter may in fact, be dry but what no one wants is moisture getting past the filter seal. If you take out the filter, is there excessive moisture in the housing or dust?
That one is fairly simple to remedy. Just unplug it and connect the wiring harness connectors back. No need to fully remove the jb4 but may want to make sure connectors/wiring are not in harm's way. Of course, no logging but I didn't see anything in the one you provided to say something major is wrong.Someone on the N54 page is fairly confident there is something wrong with the JB4 wiring or unit itself, but he has not brought forth any evidence or rationale as to why.