Had one blown when I went WOT on a highway merge

Basically shut my car down, threw plug code. Limp mode, turbos don't spool so you are on just normal engine power. I threw my stock nkg back in so i could drive. Cleared code via battery restart. Pulled plug had its ceramic cracked. #3 plug.
2 months later just about the same thing, but this time no code, but if I stomped it, car would buck and throw a fit and eventually limp mode, restart would make everything normal again but turbo's wouldn't spool anymore. Pulled #6 plug thats under the ITM (Sucks), then found ceramic had actually separated into plug shaft. So had to pull the ITM off completely.
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Put 1 more Denso in just cause they are so much cheaper. Still never could WOT properly. Found that my used JB4 still had old none defaulted settings stored in it. Cleared that. Things got better, but still wasn't 100%.
Swapped to HKS, WOT all day long with/without the JB4. SMH, should have just bought the HKS's first. All this could also be 100% my fault for over tightening as I only initially installed without a torque wrench, but I don't feel I did that. (Also don't buy the wrong ones for the 3.3, got my new set for Christmas from my brother but he got me the 2.0's first.

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